by 284 » Thu Mar 27, 2008 7:14 pm
Went to lowes and all the deep sockets they had weren't deep enough.
They did have a knucklebuster (crescent wrench) that opened wide, was solid locking, and was only 8". That worked.
Put on the new one and it does the same thing, only more rapidly and doesn't go as high on the analog PSI scale. Oh well, tried to save money, but as usual, didn't work out.
So, here's my future:
1. Put said mechanical gauge on it. Problem goes away, I'm good.
If not,
2. drain oil and keeping plug off, run a gallon down it to see if it washes out anything. Reattach and refill. If problem goes away, I'm good.
if not,
3. Lower the pan and with a garden type spray pump and no nozzle, spray in a couple of quarts of Seafoam. (I use this because it's less viscous, so should aid in "cleaning out" the pan and any dingleberries). Problem goes away, I'm good.
if not...
4. Purchase a 12 pack of PBR, put milwaukee radio by vehicle, take rented engine hoist and disconnect everything I need to to raise the engine enough to pull the pan.
So.....whatchall think of that?
Last edited by
284 on Thu Mar 27, 2008 7:52 pm, edited 1 time in total.
91.5 D250, 518, stock.